Rear catches on, tailgate gutted, loom stripped further and some plastic removed taking the cup down to its lightest so far (~1125kg dry)
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Had Goodwood yesterday, good news is the car felt great, could really feel the difference with the new wheel and was going around the quickest I have ever been by the second session. Bad news is that 12 laps into the morning and the clutch started playing up
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Came in to bleed before testing on the road, was obvious at this point that bleeding helped but then slowly got worse. Went and saw Garry (Clio Man) to pressure bleed and try and save the afternoon, this made things much better on the road but as soon as I started changing at higher revs it just doesn’t want to get out or in to gear. Similar to last time no evidence of a leak or air and the box itself feels good pointing to clutch disengagement. Alex got in contact and he is confident that it isn’t the slave (has been changed twice already) so the only thing left to change is the clutch master, he has one on the shelf so is going to send (legend) Praying that this fixes things as I am not keen to have the box out again…
Potential full race car conversion in the planning stage but will save that for another post...
Mega work, really cool build! About to tackle the boot aerocatches this weekend myself. Going to gut the door as well and have the same brackets. How did you fix them to the inside and did you fix those first and mark the pin holes/catches from there?