Well it’s been awhile since Iv been on here so here’s abit of an update.
When I got back from spa I was pretty deflated as I couldn’t fully enjoy the day due to the car just locking up etc (down to poor driving and slippery conditions) and my clutch giving up and not being able to select any gears.
When I got home I removed the livery as I wasn’t 100% on it after the trip and I’m liking the blacked out look atm. I then set about dropping the gearbox to see what was going on. Turned out the pressure plate bolts had come lose (garage who fitted the new clutch and gripper didn’t use lock tight) while it was off I decided to fit a new slave and clutch just incase.
The car was then working as it should and all seemed good so got around to a few jobs like hard wire the go pro in fit a few USB ports and my carbon footrests etc
Next up was snetterton with some
Of the lads who went to spa.
I finally got a chance to drive the car properly in the dry. I really enjoyed snetterton and would defiantly go back.
The car just worked how I wanted it to few suspension adjustments to get rid of some of the understeer which defiantly helped but found with the heat of the track the tyres would just wash out.
Here’s a few pics with @rupes
After snetterton and going out with James and his beast of a meg i decided I needed more power. I didn’t want to do what everyone else has done and go with a meg engine, I decided I wanted to go with a rotrex supercharger.
I got a friend to 3D Print me one to use for mock up
I’m wanting to be abit different to the other supercharged Clio’s so making my bracket slightly different to the rest. I’m now waiting on my friend to 3D print my bracket to make sure all is good.
Since snetterton Iv had my inlets ported and gas flowed and my throttle body ported and gas flowed.
When I took the inlets off I noticed my top loom was damaged so I replaced the 2 damaged cables and re wrapped the loom
Pretty big update will try to keep it on track going forward.
Sent from my iPhone using Tapatalk